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Time-Accurate Unsteady Flow Simulations Supporting the SRM T+68-Second Pressure Spike Anomaly Investigation (STS-54B)Time-accurate unsteady flow simulations are being performed supporting the SRM T+68sec pressure 'spike' anomaly investigation. The anomaly occurred in the RH SRM during the STS-54 flight (STS-54B) but not in the LH SRM (STS-54A) causing a momentary thrust mismatch approaching the allowable limit at that time into the flight. Full-motor internal flow simulations using the USA-2D axisymmetric code are in progress for the nominal propellant burn-back geometry and flow conditions at T+68-sec--Pc = 630 psi, gamma = 1.1381, T(sub c) = 6200 R, perfect gas without aluminum particulate. In a cooperative effort with other investigation team members, CFD-derived pressure loading on the NBR and castable inhibitors was used iteratively to obtain nominal deformed geometry of each inhibitor, and the deformed (bent back) inhibitor geometry was entered into this model. Deformed geometry was computed using structural finite-element models. A solution for the unsteady flow has been obtained for the nominal flow conditions (existing prior to the occurrence of the anomaly) showing sustained standing pressure oscillations at nominally 14.5 Hz in the motor IL acoustic mode that flight and static test data confirm to be normally present at this time. Average mass flow discharged from the nozzle was confirmed to be the nominal expected (9550 lbm/sec). The local inlet boundary condition is being perturbed at the location of the presumed reconstructed anomaly as identified by interior ballistics performance specialist team members. A time variation in local mass flow is used to simulate sudden increase in burning area due to localized propellant grain cracks. The solution will proceed to develop a pressure rise (proportional to total mass flow rate change squared). The volume-filling time constant (equivalent to 0.5 Hz) comes into play in shaping the rise rate of the developing pressure 'spike' as it propagates at the speed of sound in both directions to the motor head end and nozzle. The objectives of the present analysis are to: (1) capture the dynamic responses of the motor combustion gas flow to correlate with available low-frequency (less than 12.5 sample/sec) data and (2) observe the high-frequency (up to 50 Hz) characteristics of the response to determine any potentials for dynamic coupling.
Document ID
19950017230
Acquisition Source
Headquarters
Document Type
Conference Paper
Authors
Dougherty, N. S.
(Rockwell International Corp. Huntsville, AL., United States)
Burnette, D. W.
(Rockwell International Corp. Huntsville, AL., United States)
Holt, J. B.
(Rockwell International Corp. Huntsville, AL., United States)
Matienzo, Jose
(NASA Marshall Space Flight Center Huntsville, AL, United States)
Date Acquired
September 6, 2013
Publication Date
July 1, 1993
Publication Information
Publication: Eleventh Workshop for Computational Fluid Dynamic Applications in Rocket Propulsion, Part 1
Subject Category
Fluid Mechanics And Heat Transfer
Accession Number
95N23650
Distribution Limits
Public
Copyright
Work of the US Gov. Public Use Permitted.
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