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Wake Management Strategies for Reduction of Turbomachinery Fan NoiseThe primary objective of our work was to evaluate and test several wake management schemes for the reduction of turbomachinery fan noise. Throughout the course of this work we relied on several tools. These include 1) Two-dimensional steady boundary-layer and wake analyses using MISES (a thin-shear layer Navier-Stokes code), 2) Two-dimensional unsteady wake-stator interaction simulations using UNSFLO, 3) Three-dimensional, steady Navier-Stokes rotor simulations using NEWT, 4) Internal blade passage design using quasi-one-dimensional passage flow models developed at MIT, 5) Acoustic modeling using LINSUB, 6) Acoustic modeling using VO72, 7) Experiments in a low-speed cascade wind-tunnel, and 8) ADP fan rig tests in the MIT Blowdown Compressor.
Document ID
19990064104
Acquisition Source
Langley Research Center
Document Type
Other
Authors
Waitz, Ian A.
(Massachusetts Inst. of Tech. Cambridge, MA United States)
Date Acquired
September 6, 2013
Publication Date
January 1, 1998
Subject Category
Acoustics
Distribution Limits
Public
Copyright
Work of the US Gov. Public Use Permitted.
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